Analysis on High Rates of Scaling and Salt Accumulation of 600MW Supercritical once-through Boiler

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Abstract:

The chemistry check-ups were reviewed in the first maintenance of 600 MW supercritical once-through boiler units in Henan. Several problems were found: (1) high rates of scaling on the waterwall and economizer; (2) high rates of salt deposition on the turbine blades; (3) the formation of salt deposits on blades were complicated; (4) corrosion of low pressure turbine blades in period of maintenance was a universal phenomenon; (5) FAC (flow-accelerated corrosion) were most frequent in HP heaters and HP drain lines in most fossil plants. The reasons have been analyzed and the suggestions have been provided.

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620-626

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May 2012

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© 2012 Trans Tech Publications Ltd. All Rights Reserved

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