Failure Analysis on Tee Joint Crack of Subcritical Power Station Boiler Platen Superheater Header

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Abstract:

Failure cause analysis was carried out on tee joint crack of boiler platen superheater header (12Cr1MoV) of subcritical power station applying microanalysis, mechanical properties test, chemical composition analysis, metallography examination and SEM observation etc. Results indicated that the tee joint crack originated at the original defects, connected with reheat cracks during propagation and led to leakage finally. The improper structure, the original welding defects, overhigh welding heat input, and excessive welding residual stress resulted in the leakage failure.

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Advanced Materials Research (Volumes 538-541)

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1992-1997

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June 2012

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© 2012 Trans Tech Publications Ltd. All Rights Reserved

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