The Feasibility Experimental Study of Pumping and Shunting Pump under Pressure in Oilfield Water Injection Station

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Abstract:

In order to simplify the operation process of water injection station and improve the utilization rate of water injection. We carried out the experiment of pumping under pressure and shunting pump when installed the rotor frequency control devices. The results shows that when the start pressure ranges from 0MPa to 15MPa, the surge current of power system keeps below the maximum allowed surge current so that the water injection pump runs smoothly and the instruments and devices are in good condition. And so does the system when the pressure changes from 0MPa to 16MPa in the shunting pump under pressure experiment. By making use of the rotor frequency control devices, the station reduces the labor intensity and simplifies the operation. Besides, the utilization rate of water injection is improved.

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Periodical:

Advanced Materials Research (Volumes 616-618)

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913-916

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December 2012

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© 2013 Trans Tech Publications Ltd. All Rights Reserved

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