The Research of Gas Drainage Technology in Daning Coal Mine

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Abstract:

3# coal seam of Daning coal mine is outburst,thus severely restricting the safe production. Based on the analysis of gas emission sources and the logical drainage parameters, firstly, Daning coal mine arranged some drilling fields, then utilized the VLD-1000-type rig to drill boreholes, achieving the integrated gas drainage of the coal seam and goaf. Finally, there is a test on the drainage result. The results showed that, through this kind of integrated gas drainage technology, the highest value of gas pressure in the coal seam reduced to 0.63MPa from 1.95MPa after twelve months’ drainage, and the gas drainage rate of the whole mine reached 77.6%, achieving efficient use of gas clean energy.

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2558-2563

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July 2014

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© 2014 Trans Tech Publications Ltd. All Rights Reserved

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