Study of Cold-State Aerodynamic Field Test on the Outlet of 2150t/h Supercritical Once-Through Boiler

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Abstract:

The new unit putting into production is the supercritical boiler with a level of or above 600 MW, and most of them take the corner tangential combustion technology. The Long-term operation practice shows that there is gas temperature deviation on all the horizontal flues of boilers, which usually leads to the overheating tube burst of the high-temperature superheater and reheater, thus threats the safe and economic operation of power station. Towards the gas temperature deviation phenomenon that exists commonly in tangentially fired boiler, this paper went on the pertinent cold-state aerodynamic field test on the tangentially fired boilers in one new power plant and studied the airflow velocity at the furnace outlet in eight vertical levels by changing the SOFA horizontally rotating angle. The experiment showed that changing the baffles opening and horizontally rotating angle of SOFA air door could adjust airflow quite well and make it uniform, furthermore, the airflow can reach a basic balance at the biggest anti-tangential angle. This paper has some reference value towards improving the gas temperature deviation problem of tangentially fired boilers.

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3217-3222

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October 2013

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© 2014 Trans Tech Publications Ltd. All Rights Reserved

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