A Substation DC System Grounding Fault Analysis and Processing

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Abstract:

A 220kV substation DC system ground fault detailed analysis and lookup scheme are proposed in this paper. The ground fault was mainly due to the cold weather as well as equipment wiring unreasonable wear the cable jacket rupture, causing 220kV main transformer cooler control box on the 2nd DC grounding occurred. In addition, through this ground fault finding, also found a DC system insulation monitoring device functional shortcomings and DC circuit loop back problems exist, the paper put forward DC circuit loop back detailed solutions, and the insulation monitoring device of the transformation proposal are proposed.

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1784-1786

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February 2014

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© 2014 Trans Tech Publications Ltd. All Rights Reserved

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