Economic Analysis of Wet Flue Gas Desulfurization System with the Application of Low Pressure Economizer for Waste Heat Recovery

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Abstract:

The data of wet flue gas desulfurization (WFGD) power and water consumption, from two different coal-fired power plants (100 MW and 1000 MW) under full load operation, are studied for the WFGD economic analysis of waste-heat-recovery transformation with the installation of low pressure economizer (LPE). The results of 100MW unit show that, WFGD inlet flue gas temperature drops from 155°C to 110°C, the benefits generated include power consumption of fans declines by 23.85% and water consumption of the smoke desulfurization absorption tower declines by 34.88%. In another case, the temperature of inlet flue gas from WFGD of 1000 MW unit drops from 130°C to 84°C, power consumption of fans increases by 15.04% while water consumption of the smoke desulfurization absorption tower declines by 73.1%. Besides, the flow resistance is increased in LPE water side due to the installation of LPE. This makes power consumption of condensate pump enhanced, which slightly decreases the benefits from waste heat recovery.

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Periodical:

Advanced Materials Research (Volumes 1092-1093)

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491-497

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March 2015

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© 2015 Trans Tech Publications Ltd. All Rights Reserved

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